Well, the project is technically finished. The second z-axis bracket made it's way here. Everything is assembled and wired.
Then..I broke it.
I had a slim stepper on the Y axis, but this was honestly too much for the little guy. So I threw two of the slim ones on the Z axis (perfecto) and stole the Z axis motor as it's the same as the original Y motor, without the stupid press fittings.
I. Didn't. Swap. The. Middle. Wires. Back.
Oh yeah. It peaked above the drivers rating. Now I have no Y axis control.
This project is temporarily delayed for 2 weeks as I either arrange a new board or get brave enough and make something out of one of my RaspberryPis